Seaboard92
Engineer
It's still losing time over the road. The Meteor lost about five hours between RMT and PTB I'm guessing it or someone else hit something. And 52 lost three hours and is now four hours late again.
There were multiple issues but nothing involved any sort of collision.It's still losing time over the road. The Meteor lost about five hours between RMT and PTB I'm guessing it or someone else hit something. And 52 lost three hours and is now four hours late again.
I'm guessing there were three issues - C, S, and X.There were multiple issues but nothing involved any sort of collision.It's still losing time over the road. The Meteor lost about five hours between RMT and PTB I'm guessing it or someone else hit something. And 52 lost three hours and is now four hours late again.
One could argue that if the Auto Pain had departed on time, it would have avoided some of the issues.I'm guessing there were three issues - C, S, and X.There were multiple issues but nothing involved any sort of collision.It's still losing time over the road. The Meteor lost about five hours between RMT and PTB I'm guessing it or someone else hit something. And 52 lost three hours and is now four hours late again.
Departure from Lorton on March 6 was only 47 minutes late, but that's the best the train has been able to manage. Since Feb. 25, that consist has made 5-1/2 round trips. Remarkably fast turnarounds have helped a lot, particularly at the Lorton end, where the personnel have been able to cut the time deficit by over 3 hours on 3 separate occasions. Time has been saved at every turnaround, for a total of 25 hours and 49 minutes gained. This would have been much more than enough effort to bring the consist back to time after the 14 hour lateness. However, operations over CSX have lost a total of 13 hours and 32 minutes. That's why departure today was 1 hour and 43 minutes late. If that train loses time again on its run tonight, it will have made 6 round trips (12 one way trips) without gaining time on a single run. (Some folks say consistency is good, but I'm not convinced in this case). This is a train that historically has consistently made its "17 hour" run in less than 16 hours.
Go figure.
Tom
One could argue if the Auto train was on time, odds are it wouldn't have been delayed by this incident since it would have been ahead of 91(6).JACKSONVILLE, Fla. - A bicyclist crossing tracks on the Westside was struck and critically injured Monday morning by an Amtrak train.
According to the Jacksonville Sheriff's Office, a northbound freight train had just cleared the tracks on McQuade Street about 8 a.m. and a man on a bicycle wearing ear buds proceeded across the track while the crossing arm was still down. He was struck by the southbound Amtrak train.
I did mention the bicycle accident towards the end of my first paragraph. The 2 hours and 56 minutes lost on that southbound run is a relatively small percentage (21-1/2%) of the total time lost on CSX over the past 11 days (13 hours, 32 minutes since 2/26/16). If there had been no over-the-road delays at all, the train could have left Lorton on time as early as March 2, and we wouldn't consider the March 7 bicycle accident relevant to the discussion.
Tom
Only an hour to determine that the train in the person the engineer and conductor were not responsible. Must be some kind of record.After just over an hour, the train was allowed to proceed on its route.
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