Sad news at work today and everyone concerned for our friend!
Was curious about #92's annullment and was shocked by the info!
Early Sunday morning, a few guys were changing out a traction motor on a loco at the wheelpit area. At the same time, CSX was switching out B/O cars on #92 and #98. As been said before, CSX is contracted by Amtrak to do the switching in the yard and moving the consists to the station or to yard. Due to low seniority of engineers and conductors, we end up with the "newbies" and our yard has become a training facility against our objections.
Seems the night was off to a bad start! One consist was "spotted" after the moves and the lounge car was on the bottom of the train! :blink: Called CSX back to move cars again.
Anyway, CSX was making their moves and all moves from the "running" tracks use the "lead" track next to the wheel pit. 30 to 60 moves a day happen on this track. Being an everday occurence, everyone continues with their jobs and blocks the noise out to concentrate or hear the other workers during movement of the wheel lift.
CSX pulled a consist out of the yard, which brings the switcher and half the consist past the wheelpit. The conductor didn't properly lock the swith down and when the consist was being pushed back into the yard, "all hell broke loose!"
A coachcar near the bottom of the consist split the switch and each truck went to a different track as the engine continued to push. Everything from the coach back started to derail and rip the rail out as the cars approached the wheel pit.
One car struck the back of the loco as the guys were working under the loco. Not paying attention to the move, worker was reaching for a hydraulic jack when the loco was shoved 18 ft and the wheel of the loco sliced off the back of his arm from shoulder to elbow and broke his wrist. Thankfully it didn't damage the bone. Another guy injured his back trying to get away and was traumatized by the incident. A roof stanchion was also struck causing the pit roof to sag on one side.
With the lead blocked to the station and the loco damaged for #92, we were fortunate to get #98 out within the timeframe.
The worker's prognosis is good so far and think his arm will be OK after reconstruction and skin grafts. I'm sure alot of us at HIA will be praying for him for the next few weeks.
As expected, all the "big shots" from Amtrak and CSX were on the site within hours and anticipate changes soon. Management at Amtrak has been on CSX's ass for the last 3 months and this is the "last straw."
Pray for my friends and will keep everyone updated on his recovery.
It makes me sad, this kid is only 25-28 yrs old.
MJ
B)
Was curious about #92's annullment and was shocked by the info!
Early Sunday morning, a few guys were changing out a traction motor on a loco at the wheelpit area. At the same time, CSX was switching out B/O cars on #92 and #98. As been said before, CSX is contracted by Amtrak to do the switching in the yard and moving the consists to the station or to yard. Due to low seniority of engineers and conductors, we end up with the "newbies" and our yard has become a training facility against our objections.
Seems the night was off to a bad start! One consist was "spotted" after the moves and the lounge car was on the bottom of the train! :blink: Called CSX back to move cars again.
Anyway, CSX was making their moves and all moves from the "running" tracks use the "lead" track next to the wheel pit. 30 to 60 moves a day happen on this track. Being an everday occurence, everyone continues with their jobs and blocks the noise out to concentrate or hear the other workers during movement of the wheel lift.
CSX pulled a consist out of the yard, which brings the switcher and half the consist past the wheelpit. The conductor didn't properly lock the swith down and when the consist was being pushed back into the yard, "all hell broke loose!"
A coachcar near the bottom of the consist split the switch and each truck went to a different track as the engine continued to push. Everything from the coach back started to derail and rip the rail out as the cars approached the wheel pit.
One car struck the back of the loco as the guys were working under the loco. Not paying attention to the move, worker was reaching for a hydraulic jack when the loco was shoved 18 ft and the wheel of the loco sliced off the back of his arm from shoulder to elbow and broke his wrist. Thankfully it didn't damage the bone. Another guy injured his back trying to get away and was traumatized by the incident. A roof stanchion was also struck causing the pit roof to sag on one side.
With the lead blocked to the station and the loco damaged for #92, we were fortunate to get #98 out within the timeframe.
The worker's prognosis is good so far and think his arm will be OK after reconstruction and skin grafts. I'm sure alot of us at HIA will be praying for him for the next few weeks.
As expected, all the "big shots" from Amtrak and CSX were on the site within hours and anticipate changes soon. Management at Amtrak has been on CSX's ass for the last 3 months and this is the "last straw."
Pray for my friends and will keep everyone updated on his recovery.
It makes me sad, this kid is only 25-28 yrs old.
MJ
B)